煤炭工程 ›› 2025, Vol. 57 ›› Issue (2): 75-81.doi: 10. 11799/ ce202502011

• 施工技术 • 上一篇    下一篇

新型两堵一注封孔工艺在上向长距离穿层钻孔的应用研究

何文杰谢雄刚刘志飞   

  1. 贵州大学 矿业学院,贵州 贵阳 550025

  • 收稿日期:2024-04-03 修回日期:2024-07-01 出版日期:2025-02-10 发布日期:2025-04-28
  • 通讯作者: 谢雄刚 E-mail:414922360@qq.com

A new “two-plug-one-grout” sealing technology for long distance upward cross-layer drilling

  • Received:2024-04-03 Revised:2024-07-01 Online:2025-02-10 Published:2025-04-28

摘要:

为了解决在上向长距离穿层钻孔封孔时,封孔材料会因自身重力而很难增大密封长度,及浆液很难向上向长距离穿层钻孔上侧渗透的问题。采用新型两堵一注封孔工艺来解决。通过采用80mm直径钢管模拟钻孔,应用速凝膨胀封孔材料封孔的实验获知:速凝膨胀封孔材料充满了整个封孔段空间和囊袋,浆液紧实。对贵州省仲恒煤矿12集中巷20#煤层底板瓦斯抽放巷的现场试验研究可知:新型两堵一注封孔工艺受钻孔倾角变化的影响小,其平均瓦斯抽放浓度始终在60%以上,而两堵一注封孔工艺的平均瓦斯抽放浓度始终随着钻孔倾角的增大而减小,其最大的平均瓦斯抽放浓度也不过36.3%;新型两堵一注封孔工艺的平均瓦斯抽放浓度衰减速率小于0.02,而两堵一注封孔工艺的平均瓦斯抽放浓度衰减速率大于0.2。结果表明新型两堵一注封孔工艺比两堵一注封孔工艺更适合上向长距离穿层钻孔。

关键词:

上向长距离穿层钻孔 , 新型两堵一注”, 密封长度 , 钻孔倾角 , 平均瓦斯抽放浓度

Abstract:

In order to solve the problem that the sealing material for long-distance layer drilling upwards will squeeze out the front end plug of the drilling due to its own gravity and it is difficult to penetrate the upper side of the long-distance layer drilling upwards. Adopting a new "two plugs and one injection" sealing process to solve the problem. Through simulation experiments using 80mm diameter steel pipes to simulate drilling, it was found that the material of the sealing section filled the entire sealing space, and the slurry at the front end of the bag was tight. The on-site experimental study on the gas drainage roadway of the 20 # coal seam floor in the 12 concentration roadway of Zhongheng Coal Mine in Guizhou Province shows that the new "two plugs and one injection" sealing technology is less affected by changes in drilling angle, and its average gas drainage concentration is always above 60%. However, the average gas drainage concentration of the "two plugs and one injection" sealing technology always decreases with the increase of drilling angle, and its maximum average gas drainage concentration is only 36.3%; The average gas drainage concentration attenuation rate of the new "two plugs and one injection" sealing process is less than 0.02, while the average gas drainage concentration attenuation rate of the "two plugs and one injection" sealing process is greater than 0.2. The results indicate that the new"two plugs and one injection" sealing process is more suitable for upward long-distance drilling through layers than the "two plugs and one injection" sealing process.

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